Welltec mobilized a complete solution consisting of a Well Tractor®, Well Stroker®, Well Miller® and Well Cleaner® to the small platform offshore Indonesia.
First part of the operation was to remove the nipple profiles in order to gain access. The Well Stroker and Well Miller Nipple Profile Removal (NPR) were used and effectively removed both nipples in two runs.
With the nipple profiles out of the way, the Well Tractor and Well Miller for Scale Removal were run in hole and quickly removed the scale that was restricting access to new perforations.
Finally, the Well Cleaner was run in hole to suck up the remaining cuttings and recover them to surface for further analysis. As this was the first scale sample retrieved, the client was able to confirm what type of scale was present in the field and thus plan future interventions based on this information.
After Welltec had successfully completed the operation, the client was able to perforate the zones below the previous held-up depth and increase well production from 1.13 MMSCF to 3.8 MMSCF.
The entire operation was completed in six days with a considerably smaller footprint than alternative situations. The client’s upmost interest was to minimize damage to the formation, which Welltec® delivered by allowing the scale to be removed without disturbing the reservoir –akin to keyhole surgery.
TYPE OF WELL: 4 1/2” SINGLE COMPLETION
MAX. DEVIATION: 41.67° AT APPROX. 2,877 FT (877 M) MD
TOTAL DEPTH: 14,068 FT (4,288 M) MD
WHP: 1,000 PSI